180 t RH真空精炼炉脱硫工艺开发及应用
赵家七,蔡小锋,邹长东
江苏省沙钢钢铁研究院,江苏 张家港 215625
Development and application of desulfurization process for 180 t RH vacuum refining furnace
ZHAO Jia-qi,CAI Xiao-feng,ZOU Chang-dong
(Institute of Research of Iron and Steel, Jiangsu Province(Shasteel), Zhangjiagang 215625, Jiangsu, China)
摘要 针对铝镇静无取向硅钢成品硫质量分数超标问题,开发了RH脱硫工艺。通过选择合适的脱硫渣系以及工艺参数,使RH工位脱硫率达到30%~60%,W800系列无取向硅钢成品[w([S])≤]0.005 0%,达标率由72.19%提高至98%以上,同时确保了RH出钢[w(T[O])]<0.002 0%,[w([N])]<0.001 5% 。通过转炉出钢和RH过程炉渣脱氧改质,将RH出钢渣中[w((TFe))]控制在3%以下,RH过程炉渣碱度保持在5.0以上,使渣-钢之间硫的分配比达到80~260,有助于提高RH脱硫效果。
关键词 :
无取向硅钢 ,
RH真空炉 ,
脱硫剂 ,
钢包渣
Abstract :The desulfurization technology in the RH process was developed to reducethe sulfur mass percent in the non-oriented silicon steel. The desulfurization degree was controlled at 30%-60% in a RH reactor, and the ratio of in the W800 non-oriented silicon steel with[w([S])≤0.005 0%] was increased from 72.19% upto 98%. Meanwhile, this process was able to ensure that [w(T[O])<]0.002 0% and[w([N])<]0.001 5% at the end of the RH treatment. Through the slag deoxy-modification during the tapping and the RH treatment,[w((TFe))]at the end of the RH treatment was controlled below 3%. The slag basicity was kept above 5.0, and the sulfur distribution ratio between slag and steel was controlled at 80-260,which is favored to the improvement of the desulfurization process in the RH treatment.
Key words :
non-oriented silicon steel
RH vacuum furnace
Desulfurizer
Ladle Slag
收稿日期: 2018-03-28
出版日期: 2018-11-20
[1]
Boc I. Correlation of Aluminum Content Inclusion Structure and Core Loss of Non-oriented Electrical Steel[J]. Appl. Phys. 1986,64(10):53-50.
[1]
Boc I. Correlation of Aluminum Content Inclusion Structure and Core Loss of Non-oriented Electrical Steel[J]. Appl. Phys. 1986,64(10):53-50.
[2]
吴爽,樊立峰,毛一标,等.高牌号无取向电工钢中硫化物、氮化物析出的热力学分析[J].冶金丛刊,2009,180(2):13-15.
[2]
吴爽,樊立峰,毛一标,等.高牌号无取向电工钢中硫化物、氮化物析出的热力学分析[J].冶金丛刊,2009,180(2):13-15.
[3]
Okada Y, FukagawaS, ledaK, et al.Development of RH Powder Top Blowing Process[J].ISIJ,1994,80(1):9-12.
[3]
Okada Y, FukagawaS, ledaK, et al.Development of RH Powder Top Blowing Process[J].ISIJ,1994,80(1):9-12.
[4]
区铁,刘振清,刘良田,等.RH装置的粉剂顶吹脱硫[J].钢铁,2006,41(2):250-255.
[4]
区铁,刘振清,刘良田,等.RH装置的粉剂顶吹脱硫[J].钢铁,2006,41(2):250-255.
[5]
艾立群,蔡开科.RH处理过程钢液脱硫[J].炼钢,2001,17(3):53-57.
[5]
艾立群,蔡开科.RH处理过程钢液脱硫[J].炼钢,2001,17(3):53-57.
[6]
徐匡迪.关于洁净钢的若干基本问题[J].金属学报,2009,45(3):257-269.
[6]
徐匡迪.关于洁净钢的若干基本问题[J].金属学报,2009,45(3):257-269.
[7]
区铁,周国治,刘建功.RH法的脱碳及脱硫速率[J].炼钢,2000,16(2):57-62.
[7]
区铁,周国治,刘建功.RH法的脱碳及脱硫速率[J].炼钢,2000,16(2):57-62.
[8]
赵家七,邹长东,耿涛,等.炉渣脱氧改质工艺对铝镇静硅钢总氧含量的影响[J].炼钢,2016.32(2):12-17.
[8]
赵家七,邹长东,耿涛,等.炉渣脱氧改质工艺对铝镇静硅钢总氧含量的影响[J].炼钢,2016.32(2):12-17.
[9]
邹长东,耿涛,周彦召,赵家七,等.沙钢管线钢LF精炼的低成本深脱硫工艺[J].钢铁,2012.47(11):36-40.
[9]
邹长东,耿涛,周彦召,赵家七,等.沙钢管线钢LF精炼的低成本深脱硫工艺[J].钢铁,2012.47(11):36-40.
[10]
Ogura Y, Kikuchi Y, Hasegawa T, et al. Development of Secondary Refining Process and Its
[10]
Ogura Y, Kikuchi Y, Hasegawa T, et al. Development of Secondary Refining Process and Its
Application to Production of Clean Steel [J]. Tetsu-to-Hagane, 1986, 72 (9): 1309-1315.
Application to Production of Clean Steel [J]. Tetsu-to-Hagane, 1986, 72 (9): 1309-1315.
[11]
Endoh K, Kaneko T,Nagata S, et al. Effect of MgO content in CaO-CaF2 based flux on desulphurization of steel[J].ISIJ,1986,72(12):1108.
[11]
Endoh K, Kaneko T,Nagata S, et al. Effect of MgO content in CaO-CaF2 based flux on desulphurization of steel[J].ISIJ,1986,72(12):1108.
[12]
于学斌,时启龙,陈清泉,等.RH用新型脱硫剂的开发[J].炼钢,2006,22(4):51-54.
[12]
于学斌,时启龙,陈清泉,等.RH用新型脱硫剂的开发[J].炼钢,2006,22(4):51-54.
[13]
张才贵,吴旭峰,韩乃川.预熔型RH脱硫剂的开发与应用[J].炼钢,2009,25(6):26-28.
[13]
张才贵,吴旭峰,韩乃川.预熔型RH脱硫剂的开发与应用[J].炼钢,2009,25(6):26-28.
[14]
Endoh K, Kaneko T,Nagata S, et al. Effects of some factors on desulphurization by RH-injection method [J].ISIJ,1986,72(4):263.
[14]
Endoh K, Kaneko T,Nagata S, et al. Effects of some factors on desulphurization by RH-injection method [J].ISIJ,1986,72(4):263.
[1]
李兆振, 宋新莉, 刘静, 程朝阳, 毕云杰, 贾涓. 铬、锰及退火温度对无取向硅钢组织性能影响 [J]. 钢铁, 2020, 55(5): 80-86.
[2]
刘青松, 裴英豪, 施立发, 夏雪兰, 何志坚, 程国庆. 退火张力对Fe-3.0%Si无取向硅钢磁各向异性的影响 [J]. 钢铁, 2020, 55(4): 95-99.
[3]
朱诚意1,2,黄罗翼1,2,罗小燕1,2,刘玉龙1,2,汪勇1,2,李光强1,3. 钙处理对成品无取向硅钢夹杂物特性的影响 [J]. 钢铁研究学报, 2020, 32(2): 117-128.
[4]
印传磊, 杨丽梅, 田春阳, 马建超. KR铁水脱硫剂逸散及搅拌器黏渣分析 [J]. 钢铁, 2020, 55(1): 34-37.
[5]
曾建华,张敏,吴国荣,谢鑫. 30Cr13不锈钢冶炼过程夹杂物控制技术 [J]. 钢铁, 2019, 54(8): 43-47.
[6]
林朝阳 朱德庆 郭正启. 废脱硫剂在铁矿烧结中的应用 [J]. 钢铁研究学报, 2019, 31(3): 272-279.
[7]
程 林,胡志远,庞炜光,赵晓东,刘龚涛,侍爱臣. 无取向硅钢夹杂物分布及对带钢性能一致性的影响研究 [J]. , 2019, 44(1): 44-48.
[8]
李 娜,代 威,王永强,李凯轮,项 利,仇圣桃. 铈对2.9%Si-0.8%Al无取向硅钢再结晶组织和织构的影响 [J]. , 2018, 53(10): 67-73.
[9]
李娜 ,陆勤阳,王永强,朱正海 ,项利,仇圣桃. Ce对29%Si-08%Al无取向硅钢夹杂物变质的影响 [J]. 中国钢铁期刊网, 2017, 29(7): 570-576.
[10]
熊文涛,郭德福,丁美良,孙 林. 冷轧无取向硅钢纵向厚度精度优化控制方法 [J]. 钢铁, 2017, 52(4): 49-54.
[11]
龚 坚,王现辉,黎先浩,朱江波,赵艳宇,包燕平. 冷轧无取向硅钢表面白线缺陷成因分析与控制 [J]. 钢铁, 2016, 51(1): 46-51.
[12]
熊文涛,郭德福,丁美良,孙 林. 冷轧无取向硅钢横向厚度差控制技术 [J]. 钢铁, 2016, 51(1): 65-69.
[13]
赤小浩,李康伟. 无取向硅钢精炼过程夹杂物控制研究 [J]. 中国钢铁期刊网, 2016, 41(1): 14-17.
[14]
彭其春,邱雷,邹健,彭明耀,张亮洲,周剑丰. 无取向硅钢W800生产过程中夹杂物演变规律 [J]. 钢铁, 2015, 50(8): 34-38.
[15]
曾亚南, 孙彦辉, 蔡开科, 徐 蕊. RH精炼工艺对无取向硅钢MgO·Al2O3夹杂物演变影响及控制 [J]. 钢铁, 2014, 49(9): 38-43.