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800 MPa级水电钢板探伤不合分析与工艺优化

Cause analysis and process optimization of unqualified ultrasonic flaw detection for 800 MPa hydroelectric steel plate

  • 摘要: 为找出800 MPa级水电钢板探伤合格率低且不稳定的原因,本研究对轧制后探伤不合的钢板进行取样,并通过光学显微镜、扫描电镜、能谱仪进行检测。研究表明,钢板内部裂纹是探伤不合的直接原因,裂纹的长度随着钢板中B类夹杂物级别的升高而增加,浇次头、尾罐连铸坯轧制的钢板出现裂纹的长度是中间罐次的2倍;探伤不合的钢板内部出现较严重的P、S以及微合金元素偏析富集现象。在此基础上,对800 MPa级水电钢的冶炼工艺及钢种成分进行优化控制,使钢板探伤合格率由95.6%提升至98.6%,波动区间由92.5%~98.8%稳定至96.8%~99.5%。

     

    Abstract: In order to identify the reasons for the low and unstable qualified rate of flaw detection of 800 MPa hydroelectric steel plates, in this study, samples were taken from the steel plates that did not meet the flaw detection requirements after rolling, and the samples were detected by optical microscope, scanning electron microscope and energy spectrometer. Research shows that internal cracks in steel plates are the direct cause of non-conformity in flaw detection. The length of the cracks increases with the increase of the grade of Class B inclusions in the steel plates. The length of the cracks in the steel plates rolled from the continuous casting billets of the first and last castings is twice that of the middle castings. Severe segregation and enrichment phenomena of P, S and microalloying elements occurred inside the steel plates that did not meet the flaw detection requirements. On this basis, the smelting process and steel grade composition of 800 MPa hydroelectric steel were optimized and controlled, increasing the qualified rate of steel plate flaw detection from 95.6% to 98.6%, and stabilizing the fluctuation range from 92.5%-98.8% to 96.8%-99.5%.

     

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